There has been major progress this past week and the car is now running properly!
Ten days ago I removed the drivetrain with the motor going to the machine shop for balancing, and the transmission to the shop for repairs. Gilbertson Machine discovered that both the flywheel and clutch were not balanced. The flywheel had a bunch of holes drilled in it to make it turn true, and the clutch had some metal soldered on to balance it. They then reassembled the unit and it purrs like a kitten. This was worth the $150 it cost. As I mentioned in my last post, I should have done this earlier.
Chuck’s Volkswerks did the transmission work. It was re-geared to match the electric drive which has more torque than the old gasoline engine. First gear remains, what used to be 3rd is now 2nd, the old 4th is now 3rd, and a bigger gear was installed as 4th. The shop cleaned and painted the whole unit, and also fabricated a plate to cover up the starter hole. My tape offended his sensibilities, although it was doing the job. His cover looks much nicer. The work cost $525 and he even delivered it to my house on Saturday.

Starter hole cover
Finally, the Fab Shop made up some stouter motor mounting spacers for me, and didn’t even charge for it (thanks Dan and Eric!)
On Wednesday and Thursday, Travis formerly of EV Components, came over to help fix the BMS. We discovered many problems. Some of the strings of boards were backwards – the positive end must go at the most positive end of each battery bank. The connectors must be assembled so that specific colored wires are to the left side of the connector housing. Neither of these things is obvious from the documentation. Also I had not done a perfect job inserting all the tiny Molex connectors into the plastic housings. We rewired one bank to the specification and it worked. I was much relieved. I have since redone 5 other banks although I’ve not had time to confirm that they work yet. There are a further three in the back to be rewired, and three in the front – I have ordered parts to complete these.
Travis also figured out how to properly wire the BMS so it will control the charger and motor. Adding two relays and some more wires allows the BMS to shut off the charger if the batteries are getting too full. I’m still waiting on an obscure connector to finish this piece. Some wiring to the existing relays allows the BMS to shut off the motor if the batteries get too low.
So – pending some parts, the BMS is now working and I’ll shortly be able to recharge the battery pack with confidence that no damage will result.
I reinstalled the drivetrain using the new motor mounts, balanced flywheel and clutch, and rebuilt transmission. The car runs perfectly! We took it out for a test drive and there is no shaking and no noise. It goes 35mph in second gear without using all the pedal, and I took it to 45mph in third but couldn’t go faster since I was on a city street. Next up is to get out on the freeway to see how it does at higher speeds. But indications are that it will go at least 65mph without difficulty. The car has been driven 59 miles so far and has more than half its charge left. None of this has been at highway speeds, nor have we hit any challenging hills. So its not yet possible to say what the range will be. But for around-town driving only, I’m guessing it will be 100 miles or more. We’ll know more as we drive it more.
Remaining items: charger connector, BMS final wiring and testing, battery cover fabrication and installation, DC/DC converter, wiring grommets in a couple spots, spray foam into the various holes, carpet the trunk, make spare keys, and install a heater. But none of this prevents us from driving the car any time we want!
My next post will recap the cost of the project and what I’ve learned about the car’s performance. I hope to also report that the last tasks have been completed.